dc.identifier.citation | Ailing, C. 2009. Facility Layout Improvement Using Systematic Layout Planning (SLP) and ARENA. Universiti Teknologi Malaysia. Banks, C., and N. Nelson. 2010. Discrete-Event System Simulation 5th Edition. New Jersey : Pearson Education, Inc. Baskoro, Y.A. 2010. Plant Relocation of PT. Sanken Argawidjaja by Using Systematic Layout Planning (SLP) Combine with Flow Analysis and Assembly Process Design. Department of Industrial Engineering, Swiss German University, Bumi Serpong Damai. Hopp, W.J. and M.L. Spearman. 2008. Factory Physics 3rd Edition. Singapore : McGraw – Hill Companies, Inc. Kitriastika, V. 2012. A Redesign Layout to Increase Productivity (Case Study : PT. Inkoasku). Department of Industrial Engineering, Swiss German University, Bumi Serpong Damai. Meyers, F.E., and M.P. Stephens. 2005. Manufacturing Facilities Design and Material Handling. New Jersey : Pearson Prentice Hall. Prawira, A.R. 2011. Analysis of Soekarno Hatta Airport Runway Capacity by Using Discrete Event Simulation Method. Swiss German University. Bumi Serpong Damai. Saerang, E.V. 2011. Analysis, Synproject and Discrete Event Simulation to Increase Productivity of Pump Packaging System. Department of Industrial Engineering, Swiss German University, Bumi Serpong Damai, 2011. Salsabil, M.R. 2010. Designing a Self Service Kiosk System to Reduce the Queuing Time of Cinema’s Customers. Department of Industrial Engineering, Swiss German University, Bumi Serpong Damai. | en_US |
dc.description.abstract | This project is conducted in Company X, a passenger cars wheel
producing company located in Sunter, North Jakarta. With a view of increasing
the productivity of the company, the focus of this project will be redesigned the
layout of the factory. The main problem encountered is that the goods are not
produced in single location, causing a considerable hindrance in terms of time
and distance, and hence efficiency. The redesigning layout process will use SLP
method and flow analysis while supported by analysis of assembly line balancing
to optimize the layout. Regarding the evaluation process, ARENA software will
be used to simulate and identify the bottleneck in the production process, and
comparing the layout alternatives to decide the best layout. The best chosen
layout according to the simulation and SLP method that supported with flow
analysis and assembly line balancing will be used as the master draft layout that
will be proposed to Company X. | en_US |